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View Full Version : She finally had enough


907DAVE
Wed, December 30th, 2009, 07:08 PM
and let go of a rod........... on my way home for lunch today. What a horrible noise! Sucks because I was accelerating VERY slowly and had just up-shifted into second gear and bang.

I will be filling out the survey after the teardown to determine what actually failed.

88Racing
Wed, December 30th, 2009, 07:51 PM
Sorry to hear about that!
Find any block windows?

907DAVE
Wed, December 30th, 2009, 07:52 PM
ohh yeaa.........either #1 or #2 rod broke and took out both sides of the block:cry-blow:

cleatus12r
Wed, December 30th, 2009, 07:56 PM
DAMN IT!!

That really sucks Dave. Hey, I'll email you some stuff when I get a chance. I'm not "batchin' " it tonight (wife's been gone 2 nights) so I may not get right to it.

If'n you need something let me know. I have some spare parts.

88Racing
Wed, December 30th, 2009, 08:02 PM
Oooowieee!

Short block time and beef it up!
That is if other internal parts didn't get wacked too!

907DAVE
Wed, December 30th, 2009, 08:29 PM
Well if I am gonna rebuild it it will get all the goodies, I am not gonna have this happen again. Just might take awhile to get the funds, and probably going to have to sell some stuff.:cursin:

Might have to be a quitter and get someting else.

907DAVE
Thu, December 31st, 2009, 04:20 AM
I want to thank Bill for his call regarding my engine! It was 2:30 AM his time and he offered to analyze my current and not so current programming.

All I can say is WOW , you guys rock! I am so glad people like Bill, Corey, and Cody still exist in the world today, people who are willing to help out strangers without thinking twice.......my hats off to you.
















Now get some sleep:D

JWBFX4
Thu, December 31st, 2009, 12:13 PM
Well that sucks, hope you get it built back much stronger :2thumbs:

907DAVE
Thu, December 31st, 2009, 05:08 PM
Well the good news is that tuning doesn't seem to have contributed to the failure. Don't know what exactly failed yet, but makes me feel better knowing it wasn't the programing.

Thank you Bill for helping out, and for all your cool computer programs!

907DAVE
Thu, December 31st, 2009, 10:51 PM
Got the new block ready to go to the machine shop to get boiled and magged.........hopefully its OK.





http://i619.photobucket.com/albums/tt274/907dave9/Engine%20Pics/IMG_4368.jpg






Any one know what to look for when checking block casting for cavitation around the main webbing? I got lots of pic's.

Driximus
Tue, January 5th, 2010, 06:36 PM
Hope it all works out for yah. Sounds exactly what mine did its a pretty disconcerning noise :confused:

907DAVE
Sat, January 9th, 2010, 12:20 AM
Got her in the shop tonight to warm up, and will be pulling the engine tomorrow.

Here's a few pic's.........



http://i619.photobucket.com/albums/tt274/907dave9/IMG_4385.jpg





http://i619.photobucket.com/albums/tt274/907dave9/IMG_4379.jpg






http://i619.photobucket.com/albums/tt274/907dave9/IMG_4374.jpg







After looking through the hole in the block it looks like the #2 rod broke right below the wrist pin, and is still strait and bolted to the crank.......

88Racing
Sat, January 9th, 2010, 12:50 AM
Keep the pix coming!
You may have to hire a photographer so you don't get your camera dirty!
J/K!!!
LOL's

907DAVE
Sat, January 9th, 2010, 12:55 AM
Should be some carnage pic's tomorrow...........:(

907DAVE
Sat, January 9th, 2010, 09:24 PM
Todays pic's







http://i619.photobucket.com/albums/tt274/907dave9/IMG_4386.jpg







http://i619.photobucket.com/albums/tt274/907dave9/IMG_4392.jpg






http://i619.photobucket.com/albums/tt274/907dave9/IMG_4394.jpg

907DAVE
Sat, January 9th, 2010, 09:28 PM
And here the carnage...........





http://i619.photobucket.com/albums/tt274/907dave9/IMG_4398.jpg







http://i619.photobucket.com/albums/tt274/907dave9/IMG_4402.jpg








http://i619.photobucket.com/albums/tt274/907dave9/IMG_4409.jpg















:cry-blow::cry-blow: :cry-blow:

907DAVE
Sat, January 9th, 2010, 09:31 PM
And the piston.................







http://i619.photobucket.com/albums/tt274/907dave9/IMG_4412.jpg

















Pretty nice spray pattern thought................















http://i619.photobucket.com/albums/tt274/907dave9/IMG_4413.jpg

907DAVE
Sat, January 9th, 2010, 10:03 PM
And a big hole...........





http://i619.photobucket.com/albums/tt274/907dave9/IMG_4407.jpg

907DAVE
Sat, January 9th, 2010, 10:06 PM
After analyzing the rod, it appears it had cracked, and kept cracking until the last 1/8 inch , then broke completely. You can see it in the piston pic's.


hmmm...........

cleatus12r
Sun, January 10th, 2010, 09:22 AM
You're right about the spray pattern.

Again, if you need any parts, I have quite a few (front cover, oil pan, pickup, etc.)

907DAVE
Sun, January 10th, 2010, 05:04 PM
Thanks Cody! I will let you know if I need anything.:thumbs up yellow:

907DAVE
Sun, January 17th, 2010, 01:57 AM
Good news, my block came back from the machine shop with a clean bill of health. No cracks, and will need to be bored .030 and will need one sleeve. So I will be filling the block next week, then sending it back to the machine shop for them to finish up when the rest of my parts show up.

hayjayhorses
Mon, January 18th, 2010, 12:17 AM
I take it the rods must be powder metal (did I say that right?).

I blew a 7.3 a few years ago, it had over 600,000 miles on it. Well realy starting fluid did, it a cracked a piston.

I rebuilt a 2001 7.3 last year every thing new from turbo to oil pan and I have it sitting in storage in case one of my 7.3 lets go.

907DAVE
Mon, January 18th, 2010, 01:39 AM
Nope, they were forged rods that I polished, and had the machine shop magnaflux, shot peen, and heat treat.





I think they must have had a hard life in their previous engine.