|
1999 to 2003 7.3L Power Stroke Diesel 7.3L Power Stroke Diesel equipped Super Duty and Excursion. |
|
Thread Tools | Display Modes |
|
#1
|
|||
|
|||
Almost back together!
Ok guys I'm about to go from to ..... Tomorrow we are bringing my truck down to the beautiful town of Winder, GA to let Bill and Brad yank the engine out and show it some loving.... It's getting studs,Adrenaline HPOP,dieselsite fuel system, injectors and a gtp38r among other things. This isn't going to be a overnight thing but I know it will be worth the wait, especially since I havnt driven the truck in prob 2 months. I will post some pictures tomorrow of it once we get it loaded on the trailer and behind the Dodge that will be pulling it I know I know but that will hopefully be the only time it is behind it haha anyway just posting my excitement lol hope everyone has a good one!
Last edited by Lowdown89; Fri, April 29th, 2011 at 09:57 PM. |
#2
|
|||
|
|||
Haha yeah I'm bad about getting sidetracked, i have lots ofmthings that only take a few minutes that have yet to get done! I don't think he left a blanket but then again I could be wrong lol
|
#3
|
|||
|
|||
Wow bud, I can feel you excitement along with my jealousy...lol Should be sweet
__________________
2000 F-250 SCLB 2wd 7.3 auto PHP stock-65t-80dd-120race-high idle-no start 4"tb exh, wicked wheel, 3 guages, AIS, coolant filt, |
#4
|
|||
|
|||
ok, usually im always taking pictures but ended up taking 2 lol so heres one of my dually on the trailer on the way down to PHP and one of the tow rig which is my buddies 07.5 megacab.... for as nasty as the weather was sunday morning it sure turned into a nice day
|
#5
|
|||
|
|||
brad sent me a couple of pics this afternoon.... i would say its a safe bet that my old turbo is trashed.. LOL here is a pic of the carnage
|
#6
|
||||
|
||||
Awesome!
__________________
|
#7
|
|||
|
|||
the damage wasnt contained to just the turbo it got some of the pistons along with other stuff as well here is a pic of the damage to one of the pistons
|
#8
|
|||
|
|||
i was gonna say all that metal had to go somewhere, ouch, hows the rest of the head?
__________________
2002 7.3 F250 Supercab Shortbox DIY intake CCV dumped Autometer gauges WW/ATS 1.0 exhaust housing Hutch/Harpoon in tank mods/hpX line AIH delete/ebpv delete TruCool trans cooler Straight piped PHP FU |
#9
|
|||
|
|||
The valves got pretty ate up to, I had bought 2 other sets of heads so hopefully the machine shop can make something out of all the parts.... I can't say enough to bill and brad and Cody, I'm sure they will be tired of messing with my junk soon lol... At least I know when it's back together it's going to run like it's supposed to!
|
#10
|
||||
|
||||
At least your new engine will have forged rods instead of PMRs.
My big hang-up at the moment revolves around the kind of usage that spare short block you brought in has seen in it's remanufactured life....... All of the second compression rings were stuck, two of the pistons had broken ring lands, and the cylinder walls were flat WORN OUT.
__________________
Tuning, flashing, burning chips, and repairing all aspects of 7.3L Powerstrokes. SEVEN 7.3L-powered vehicles in the driveway. Two didn't come that way from the factory! |
|
|