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1999 to 2003 7.3L Power Stroke Diesel 7.3L Power Stroke Diesel equipped Super Duty and Excursion. |
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#1
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I may have found my loss of power (WITH PICS)
I still really need help, so thanks for all I've gotten and will get. I didn't mention this earlier because I was waiting until I could get home and snap a few pics, but I noticed what looks like a missing bolt on the intake plenum. See pics here:
The pics are progressively zooming in I hope you can see in the pics what bolt I'm talking about. And if I am correct, I would think this bolt would definitely hold in some sort of pressure, especially under heavy loads. Please let me know what y'all think. If that is a missing bolt, does anyone know what size and thread the bolt is that I need to get to replace it??? Thanks.
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Bob- 2003 F250 Lariat 7.3PSD CC SB FX4 Kwik (6637) Filter, RE 2.5" leveling kit, F350 Rear Blocks, TC Lock, Fumoto, EBPV/Exhaust Brake,6.0 Tranny Cooler, AIH Delete, IssPro EV2 Gauges, PHP Phoenix stock, 25tow, 40tow, 65tow, 80dd, 100perf, In-tank mods, Muffler Delete, WW, FRx,HPx, JW Stage 1 Trans, Swamps HV/HF IDM -Pulling a 38' Forest River Sierra 5th Wheel |
#2
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Bob, I can send you the bolt (I have a ton of extras) but being that I have removed quite a few of those, I can say with near absolute certainty that the sealant that holds those plenums on is nearly bulletproof and a leak there would be REALLY wet with oil....not just a bit damp and dirty like yours is. In addition, the bolt hole is a "blind" hole which means that it doesn't go through the casting into a place where it will leak through the bolt hole.
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Tuning, flashing, burning chips, and repairing all aspects of 7.3L Powerstrokes. SEVEN 7.3L-powered vehicles in the driveway. Two didn't come that way from the factory! |
#3
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Cody, what if I was to tell you that even though there isn't much oil right there, I do have quite a bit of oil in the valley and all over the backside of the engine, and it's new, since the last couple of weeks.
I was actually trying to figure out where that was coming from, too, but haven't had any luck yet. Iisnt it possible that all these things are connected? Increased noise, loss of power under load, everything sprayed with oil, and now this missing bolt????
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Bob- 2003 F250 Lariat 7.3PSD CC SB FX4 Kwik (6637) Filter, RE 2.5" leveling kit, F350 Rear Blocks, TC Lock, Fumoto, EBPV/Exhaust Brake,6.0 Tranny Cooler, AIH Delete, IssPro EV2 Gauges, PHP Phoenix stock, 25tow, 40tow, 65tow, 80dd, 100perf, In-tank mods, Muffler Delete, WW, FRx,HPx, JW Stage 1 Trans, Swamps HV/HF IDM -Pulling a 38' Forest River Sierra 5th Wheel |
#4
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I suppose it's possible....as is anything. I am a bit concerned about just sticking a bolt in it and hoping that the silicone actually seals it up again. Once the cured silicone is ripped apart, it's no good. You can try it though!
I'll send you a bolt (you may have to send me your address again ) but I can ship it Monday. On edit: The oil that I'm noticing in the pictures is pretty common of loose clamps on the orange hoses from the "y" into the plenum. I've fixed a couple "rear main seal leaks" just by tightening those clamps.
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Tuning, flashing, burning chips, and repairing all aspects of 7.3L Powerstrokes. SEVEN 7.3L-powered vehicles in the driveway. Two didn't come that way from the factory! |
#5
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Thanks for all the help Cody. Really, if you can just tell me the particulars of the bolt then I will just go to the autoparts store and get one. They should have it, right?
I will recheck the clamp on the orange boots tomorrow. Thanks again.
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Bob- 2003 F250 Lariat 7.3PSD CC SB FX4 Kwik (6637) Filter, RE 2.5" leveling kit, F350 Rear Blocks, TC Lock, Fumoto, EBPV/Exhaust Brake,6.0 Tranny Cooler, AIH Delete, IssPro EV2 Gauges, PHP Phoenix stock, 25tow, 40tow, 65tow, 80dd, 100perf, In-tank mods, Muffler Delete, WW, FRx,HPx, JW Stage 1 Trans, Swamps HV/HF IDM -Pulling a 38' Forest River Sierra 5th Wheel |
#6
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The bolt is a 8mmX 1.25 and is 5/8 long.
The bolt that was suppose to be in there looks like this. IIRC it was for the ground wire that went to your AIH. On edit it looks like the ground wire is still there but it doesn't look like it is hooked up.....or is it? Sorry but I am with Cody on this one. |
#7
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The AIH was removed when we installed my gauges. I didn't actually do it, but my friend did. That may be when the bolt was loosened or something. My boost gauge plugs into an AIH delete plug.
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Bob- 2003 F250 Lariat 7.3PSD CC SB FX4 Kwik (6637) Filter, RE 2.5" leveling kit, F350 Rear Blocks, TC Lock, Fumoto, EBPV/Exhaust Brake,6.0 Tranny Cooler, AIH Delete, IssPro EV2 Gauges, PHP Phoenix stock, 25tow, 40tow, 65tow, 80dd, 100perf, In-tank mods, Muffler Delete, WW, FRx,HPx, JW Stage 1 Trans, Swamps HV/HF IDM -Pulling a 38' Forest River Sierra 5th Wheel |
#8
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On your oil leak....
Since you have an 03, check the two high pressure oil hose fittings that connect to the left side of the HPOP. The O-ring on those fitting can fail(especially on 02's and 03's), and can cause a valley/rearmain appearence oil leak. It can be tough to see, but it will appear to have a washed down look to it, just under each of the two fittings. You can't quite see the HPOP in your pictures.... On your bolt, I'll bet its in the Valley still, look around and fish around with a magnet. You'll probably find it.
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19 F-350 6.7 Auto 16 F-350 6.7 Auto 05 Excursion 6.0, Auto, PHP Atlas 40 FICM, ARP Studs VXBC6(truck PCM) 00 F-350 7.3, 12 Speed, PHP Gryphon, PHP hydra, DAC3 95 F-Superduty 7.3 DI, Auto, Mechanics Truck 94 F-Superduty 7.3 DI, 5 speed, Flatbed |
#9
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Alright, so I haven't had time to build a leak detector, but I had a few minutes this morning so I had the wife do a brake stand and run the truck up to about 2500rpm and 15psi of boost. I put some soapy water around the hole and there was a tad bit of bubbling, not much really. But then I put my finger over the hole and it was a steady flow of a good amount of air, and it directly correllated to the boost and rpm. When she let off the pedal, the airflow out of the hole went away. So, what do you guys think now? I would think I found my problem and need to plug the hole to fix it. But I wanted to keep y'all in the loop and get your input.
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Bob- 2003 F250 Lariat 7.3PSD CC SB FX4 Kwik (6637) Filter, RE 2.5" leveling kit, F350 Rear Blocks, TC Lock, Fumoto, EBPV/Exhaust Brake,6.0 Tranny Cooler, AIH Delete, IssPro EV2 Gauges, PHP Phoenix stock, 25tow, 40tow, 65tow, 80dd, 100perf, In-tank mods, Muffler Delete, WW, FRx,HPx, JW Stage 1 Trans, Swamps HV/HF IDM -Pulling a 38' Forest River Sierra 5th Wheel |
#10
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Put a bolt in it. If you felt air coming out of the bolt hole, then by all means, plug that bad boy up with a new bolt!!
I am wondering HOW you are getting air out of the bolt hole as both pairs of heads I have here have blind holes in that location. Maybe the casting is different or something. Regardless, that is definitely an issue!
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Tuning, flashing, burning chips, and repairing all aspects of 7.3L Powerstrokes. SEVEN 7.3L-powered vehicles in the driveway. Two didn't come that way from the factory! |
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