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1999 to 2003 7.3L Power Stroke Diesel
7.3L Power Stroke Diesel equipped Super Duty and Excursion.


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  #51  
Old Fri, December 10th, 2010, 08:15 AM
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I am running between 79 - 80 psi at the fuel filter return.
At the back of the heads I am running 76psi no load and 69 psi under full load.
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Thank you and have a great day, Troy Detweiler

I have a '99 F 250 7.3L Diesel w/ a 6 speed Tranny and 4x4.
Mods: Amsoil dual bypass oil filters, Amsoil air intake mod DIY, fuel preasure spring mod(70psi), FU Chip and Burner , 3.73 rear gears, leveling kit (DIY), Stabilizer bars on the rear axle (DIY).
'02 F 350 7.3L, 6spd,4x4,CC, Dually- Just bought 4-15-11
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  #52  
Old Fri, December 10th, 2010, 12:25 PM
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Why is the pressure so high?

Might try dropping it back down to 60.
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  #53  
Old Fri, December 10th, 2010, 12:29 PM
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We installed a different fuel pressure spring in the return. This was done over 2 years ago, to smooth out the idle, and cold weather starts. It also brought the fuel economy up just a touch. It is still with in Specs from International and ford.
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Thank you and have a great day, Troy Detweiler

I have a '99 F 250 7.3L Diesel w/ a 6 speed Tranny and 4x4.
Mods: Amsoil dual bypass oil filters, Amsoil air intake mod DIY, fuel preasure spring mod(70psi), FU Chip and Burner , 3.73 rear gears, leveling kit (DIY), Stabilizer bars on the rear axle (DIY).
'02 F 350 7.3L, 6spd,4x4,CC, Dually- Just bought 4-15-11
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  #54  
Old Fri, December 10th, 2010, 12:32 PM
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We have taken all mods off, returned the truck back to stock. The truck will run great until we install the FU Chip, then everything goes back to the bad running motor.

Just like this post:

Here is what I have done since last post.
Did the buzz test, everything sounds good on all 8 cylinders. Contribution test is good on all 8 also.
I am lost as to what is going on here.
Now the truck doesn't have the miss, but also has very low power even with the FU chip on 100 hp setting. It feels like the chip isn't even in the truck. my boost used to go to 26-28 psi now it only goes to 15 psi max, blows black smoke really bad. Even smokes on the idle, it is also black, sitting in garage for 3 to 5 minutes, when warm and idling, will burn your eyes really bad.
Oh MPG is down to average of 8.

I took the new injectors out of 7 and 8, put old ones back in, truck still has no miss, but the rest is still the same- no power, smokes on idle when warm, smokes driving it, with the FU chip in.

Take chip out and everything runs perfectly. No smoke, no miss, nothing, and has power, contribution test good, buzz test good, boost up to 26psi, 16 mpg average. I am LOST

Any ideas now? Ready to trade truck off, but can't with it running like this.

Could there be thick oil trapped in a injector boss that causes the solenoid to buzz correctly but injector not work right??????
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Thank you and have a great day, Troy Detweiler

I have a '99 F 250 7.3L Diesel w/ a 6 speed Tranny and 4x4.
Mods: Amsoil dual bypass oil filters, Amsoil air intake mod DIY, fuel preasure spring mod(70psi), FU Chip and Burner , 3.73 rear gears, leveling kit (DIY), Stabilizer bars on the rear axle (DIY).
'02 F 350 7.3L, 6spd,4x4,CC, Dually- Just bought 4-15-11
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  #55  
Old Fri, December 10th, 2010, 03:41 PM
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Guess I missed that post......

Would have to be a calibration issue then.
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  #56  
Old Mon, February 7th, 2011, 09:29 AM
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Well, IT is FIXED finally.
There was a bad calibration in the chip. I think it was from when we updated the chip burning program for the FU Chip. I wiped all programing off the computer, reinstalled and re-burnt the chip. Now everything is back to normal. Who would have figured that it was a cheap fix.
Thank you everyone for all your help in this matter, it has been a long drawn out test.
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Thank you and have a great day, Troy Detweiler

I have a '99 F 250 7.3L Diesel w/ a 6 speed Tranny and 4x4.
Mods: Amsoil dual bypass oil filters, Amsoil air intake mod DIY, fuel preasure spring mod(70psi), FU Chip and Burner , 3.73 rear gears, leveling kit (DIY), Stabilizer bars on the rear axle (DIY).
'02 F 350 7.3L, 6spd,4x4,CC, Dually- Just bought 4-15-11
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  #57  
Old Mon, February 7th, 2011, 09:30 AM
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Not sure but someone may want to put this in a sticky somewhere on this forum. There is a lot of good testing info from everyone in this thread.
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Thank you and have a great day, Troy Detweiler

I have a '99 F 250 7.3L Diesel w/ a 6 speed Tranny and 4x4.
Mods: Amsoil dual bypass oil filters, Amsoil air intake mod DIY, fuel preasure spring mod(70psi), FU Chip and Burner , 3.73 rear gears, leveling kit (DIY), Stabilizer bars on the rear axle (DIY).
'02 F 350 7.3L, 6spd,4x4,CC, Dually- Just bought 4-15-11
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  #58  
Old Mon, February 7th, 2011, 12:24 PM
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Quote:
Originally Posted by Probuilder View Post
Well, IT is FIXED finally.
There was a bad calibration in the chip. I think it was from when we updated the chip burning program for the FU Chip. I wiped all programing off the computer, reinstalled and re-burnt the chip. Now everything is back to normal. Who would have figured that it was a cheap fix.
Thank you everyone for all your help in this matter, it has been a long drawn out test.
WOW!!!

Glad its working for ya!
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  #59  
Old Tue, February 8th, 2011, 03:32 PM
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Moved from emergency....
A thread this old will be closed otherwise....
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