|
1999 to 2003 7.3L Power Stroke Diesel 7.3L Power Stroke Diesel equipped Super Duty and Excursion. |
|
Thread Tools | Display Modes |
#1
|
|||
|
|||
Can EGT probe go bad?
I got a set of GlowShift gauges on the pillar. The EGT gauge started give jumpy readings at idle. Then under acceleration, no reading. I contacted GlowShift CS and they told me I could check the gauge by disconnecting the EGT probe wiring. That caused the gauge to max out, then when I grounded it.... it bottomed out. According to GlowShift this means the gauge is working properly. I've double checked the wiring and it is all hooked up.
So I'm thinking its the EGT probe. Can these go bad? I've had it in for about a year. Is there a better replcement probe? The probe wiring just splits off into 2 wires at the end. Thanks
__________________
01 F350 7.3 4x4 CC SRW/3.73/315-75-16/Aeroforce Interceptor/BD Thruster II/ Bellowed Up-Pipes/4" turbo back exhaust/CCV Mod/DIY 6637/FPR Shimmed to 65 PSI/TS chip reburned with PHP tunes (Stock, 40T WITH Whsiper tune, 80DD, 100R, 140Ex, 140SS)/Replaced and Cleaned EBPS & Tube 4-6-12/Zoodad mod/Recon smoked cab lights/MM Hubs/Cowl Hood/HPx |
#2
|
|||
|
|||
your problem is glowshift, LOL.
yeah i'd say the probe is bad though honestly.. new thermocouple time.
__________________
2002 7.3 F250 Supercab Shortbox DIY intake CCV dumped Autometer gauges WW/ATS 1.0 exhaust housing Hutch/Harpoon in tank mods/hpX line AIH delete/ebpv delete TruCool trans cooler Straight piped PHP FU |
#3
|
|||
|
|||
I had the probe go bad on my edge juice with attitude. Sold the edge, and the guy put a new probe on it and it worked again. So the answer in my experience is yes.
__________________
2002 F250 CCSB Lariat 4x4 6637 intake 4" dp w/ muffler delete Stage 1 single shots and PHP tuning Procomp Xtreme AT 285/75r16 2 1/2 inch leveling kit |
#4
|
|||
|
|||
yes glowshit sucks not good at all cheap
|
#5
|
|||
|
|||
Okay thanks guys. The glowshift gauges have lasted me a year with no problems untill now. But just in case it's not the probe, I bought a BD X-Monitor for $70 yesterday. Just hope it works when i get it.
I may try to get another probe before I install the x-monitor just to make sure that was the problem before I get rid of the glowshift gauges, that way I can say it was working when removed from my truck.
__________________
01 F350 7.3 4x4 CC SRW/3.73/315-75-16/Aeroforce Interceptor/BD Thruster II/ Bellowed Up-Pipes/4" turbo back exhaust/CCV Mod/DIY 6637/FPR Shimmed to 65 PSI/TS chip reburned with PHP tunes (Stock, 40T WITH Whsiper tune, 80DD, 100R, 140Ex, 140SS)/Replaced and Cleaned EBPS & Tube 4-6-12/Zoodad mod/Recon smoked cab lights/MM Hubs/Cowl Hood/HPx |
#6
|
|||
|
|||
i put in a set of brand new glow shift gauges for a friend and the probe was bad, we called customer service and they even told us to try cutting off the connectors they provide with them because in his own words the connectors they use SUCK.... that still didnt fix it, so they sent us a new probe and since then it has worked fine so i would also say its a bad probe
|
|
|