Power Hungry Performance Forum  

Go Back   Power Hungry Performance Forum > Ford Super Duty & Excursion > 1999 to 2003 7.3L Power Stroke Diesel

1999 to 2003 7.3L Power Stroke Diesel
7.3L Power Stroke Diesel equipped Super Duty and Excursion.


Reply
 
Thread Tools Display Modes
  #1  
Old Wed, February 3rd, 2021, 09:43 PM
cleatus12r's Avatar
cleatus12r cleatus12r is offline
F Your Yankee Blue Jeans
 
Join Date: Jan 2009
Location: Somewhere in Montana
Posts: 2,654
cleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to all
Default 7.3 Carnage.

I rebuilt a 7.3L for a guy about a year and a half ago. It turns out that the engine had been rebuilt ALREADY just before this guy bought it.

I'll post two pictures here and let someone take a crack at what caused the failure. This was a 1000% non-fixable block as you'll see. What was the root cause of the failure?

Good luck. Winner gets.....well......to say he guessed the cause.
Attached Images
File Type: jpg 20190622_161929.jpg (404.3 KB, 29 views)
File Type: jpg 20190623_065342.jpg (294.5 KB, 33 views)
Reply With Quote
  #2  
Old Thu, February 4th, 2021, 01:47 AM
Power Hungry's Avatar
Power Hungry Power Hungry is offline
The Godfather of Power Stroke Tuning
 
Join Date: Nov 2008
Location: Winder, GA
Posts: 2,264
Power Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud of
Default

Aren't the valves supposed to be in the Cylinder Head, not the top of the piston?

My initial guess would be bad seat pressure on the springs which caused valve float. Or possible, trying to run an exhaust brake which again caused valve float.

As you indicated, that block is scrap at this point!
__________________
Bill Cohron - The Mad Doctor

Power Hungry Performance - The ORIGINAL in Ford performance tuning... Since 1997!
(678) 890-1110

www.gopowerhungry.com - Home of the Hydra Chip, Minotaur Tuning Software, and the new Orion Reflash System for Navistar!

Bring back Windows™ XP and 7.
Windows™ Vista and Windows™ 8 is a pain in my a$$!
Windows™ 10 is only slightly less annoying!
Windows™ 11 is garbage!

Much to my surprise, I'm actually quite enjoying Linux!
Reply With Quote
  #3  
Old Thu, February 4th, 2021, 08:31 AM
cleatus12r's Avatar
cleatus12r cleatus12r is offline
F Your Yankee Blue Jeans
 
Join Date: Jan 2009
Location: Somewhere in Montana
Posts: 2,654
cleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to all
Default

Yes, the valves in that particular cylinder are supposed to be in the head, not the piston.

However, they did not travel from their home due to any issue listed.

A couple more pictures:
Cylinder 6 was the initial failure and as you can see, the block is cracked at the 2 o'clock position in #6 (picture rotated 90 degrees counterclockwise) and cylinder #8 that ate some of the chunks (#6 wasn't selfish and decided to share), cracked the cylinder wall at the 2 o'clock position as well. That whole section of the block was BROKEN all the way to the lifter bores. The tuning that was flashed to the PCM long before I ever saw this thing...well...it was HOT. But that's not why it failed.



The answer will be revealed a bit later but here's another hint: There is a reason the cylinder heads were pictured side by side and keep in mind that this engine was recently remanufactured.
Attached Images
File Type: jpg 20190622_161956.jpg (349.7 KB, 20 views)
File Type: jpg 20190622_161920.jpg (292.6 KB, 15 views)
File Type: jpg 20190622_161935.jpg (474.4 KB, 14 views)

Last edited by cleatus12r; Thu, February 4th, 2021 at 12:39 PM.
Reply With Quote
  #4  
Old Thu, February 4th, 2021, 04:10 PM
Longshot270's Avatar
Longshot270 Longshot270 is offline
Forum Predator
 
Join Date: Jul 2009
Location: DFW, TX
Posts: 1,878
Longshot270 will become famous soon enough
Default

Did they spin it too fast for too long?
__________________
Reply With Quote
  #5  
Old Thu, February 4th, 2021, 08:55 PM
Power Hungry's Avatar
Power Hungry Power Hungry is offline
The Godfather of Power Stroke Tuning
 
Join Date: Nov 2008
Location: Winder, GA
Posts: 2,264
Power Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud of
Default

Oh, it looks like the intake and exhaust valves are swapped on the one head.
__________________
Bill Cohron - The Mad Doctor

Power Hungry Performance - The ORIGINAL in Ford performance tuning... Since 1997!
(678) 890-1110

www.gopowerhungry.com - Home of the Hydra Chip, Minotaur Tuning Software, and the new Orion Reflash System for Navistar!

Bring back Windows™ XP and 7.
Windows™ Vista and Windows™ 8 is a pain in my a$$!
Windows™ 10 is only slightly less annoying!
Windows™ 11 is garbage!

Much to my surprise, I'm actually quite enjoying Linux!
Reply With Quote
  #6  
Old Thu, February 4th, 2021, 09:05 PM
cleatus12r's Avatar
cleatus12r cleatus12r is offline
F Your Yankee Blue Jeans
 
Join Date: Jan 2009
Location: Somewhere in Montana
Posts: 2,654
cleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to all
Default

BINGO!

They are the same diameter and length. The seats are cut at different angles but they'll still seal. The problem? The margin becomes too narrow and the valve material is WAY different. The exhaust valve is an inconel alloy and the intake is something ferrous that is way less heat resistant.

You win, Bill!
Reply With Quote
  #7  
Old Thu, February 4th, 2021, 10:24 PM
Power Hungry's Avatar
Power Hungry Power Hungry is offline
The Godfather of Power Stroke Tuning
 
Join Date: Nov 2008
Location: Winder, GA
Posts: 2,264
Power Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud ofPower Hungry has much to be proud of
Default

Quote:
Originally Posted by cleatus12r View Post
BINGO!

They are the same diameter and length. The seats are cut at different angles but they'll still seal. The problem? The margin becomes too narrow and the valve material is WAY different. The exhaust valve is an inconel alloy and the intake is something ferrous that is way less heat resistant.

You win, Bill!
Thanks. I was trying to look at the pics on my phone earlier. Couldn't make out much detail. Now that I'm on the computer, it's much more evident.

Now with that said, maybe they confused the head with a prototype reverse-flow setup. LOL
__________________
Bill Cohron - The Mad Doctor

Power Hungry Performance - The ORIGINAL in Ford performance tuning... Since 1997!
(678) 890-1110

www.gopowerhungry.com - Home of the Hydra Chip, Minotaur Tuning Software, and the new Orion Reflash System for Navistar!

Bring back Windows™ XP and 7.
Windows™ Vista and Windows™ 8 is a pain in my a$$!
Windows™ 10 is only slightly less annoying!
Windows™ 11 is garbage!

Much to my surprise, I'm actually quite enjoying Linux!
Reply With Quote
  #8  
Old Thu, February 4th, 2021, 10:45 PM
cleatus12r's Avatar
cleatus12r cleatus12r is offline
F Your Yankee Blue Jeans
 
Join Date: Jan 2009
Location: Somewhere in Montana
Posts: 2,654
cleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to allcleatus12r is a name known to all
Default

At least one head was assembled correctly and able to be salvaged.

I bet it made one heck of a racket when it let go. The guy was pulling a trailer up a pretty good hill when it quit running.
Reply With Quote
  #9  
Old Tue, November 28th, 2023, 01:07 PM
jimcricket jimcricket is offline
Whopper Junior
 
Join Date: Nov 2023
Posts: 3
jimcricket is on a distinguished road
Default

Quote:
Originally Posted by cleatus12r View Post
At least one head was assembled correctly and able to be salvaged.

I bet it made one heck of a racket when it let go. The guy was pulling a trailer up a pretty good hill when it quit running.
curious, were you able to get the mfg/rebuild shop to cover the cost due to incorrect build?
Reply With Quote
Reply


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 10:27 PM.


All Contents Copyright 2008-2024, Power Hungry Performance