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2009 to 2014 F-150 3.5L, 3.7L, 4.6L, 5.0L, 5.4L, and 6.2L equipped F-150s. |
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Thread Tools | Display Modes |
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#1
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Did AZ load test the battery?
Was it turn key and nothing? Or turn key and it cranked with no fire? Battery voltage might have gotten to low?
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SENIOR MODERATOR--PTLA God doesn't have a Facebook but he's my friend. God doesn't have a twitter, but I follow him. |
#2
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Yeah AZ tested it.
when i would turn the key on it would make some clicking sounds really fast and the needles on my gages would shake. i dont know what it was my dad thinks its something electrical. the guy at autozone said i must of left something on but i turn everything off before i turn the truck off. |
#3
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![]() Quote:
- Jack
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2024 F150 Platinum SCrew 3.5L PowerBoost FX4, Peragon Tonneau Cover, LineX Bed, 35% Window Tint on All Sides and Rear, Full Nose Paint Protection Film, Husky Mud Guards, Lasfit Floor Liners, VIOFO Dash Cam |
#4
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I was actually thinking the same thing, about it getting charged on the way there.
A nice little fact. The milage on my truck while it was dead 6665.5 notice the first three numbers. Last edited by martinoledad; Tue, February 9th, 2010 at 11:17 PM. |
#5
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What size battery do you have?
I hope it's not Ford's dinky 550. The 650 better!
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SENIOR MODERATOR--PTLA God doesn't have a Facebook but he's my friend. God doesn't have a twitter, but I follow him. |
#6
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Yeah, that was definitely a low battery. My battery could run a high power stereo system for 5 hours but couldn't handle the key being in for 6.
![]() I dont think the battery has quite recovered yet so now when I go to events I swap it out with a 560(?) CCA deep cycle RV/Boat battery and that thing works REALLY well. Not sure if it would be good to use a deep cycle for my truck battery long term though.
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#7
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well im not sure. The truck fired up just fine this morning.
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